All posts by Sluggy

Long Overdue Update

I have done a little bit of work on Sponge Bob, but more importantly, we racked up a few miles, just short of 4000 since the new speedo was put on way back in October of 2009. Much of this is ’round town miles, though a big chunk went on in a South Texas vacation/camping trip.

Sponge Bob has a new tire as of today. I pick it up on the way home in a few minutes. I also have a new headlight that I may even get on there tonight.

Last fall, Sponge Bob’s fuel pump quit. Without realizing it, it had actually been going for a while and was misdiagnosed as an ignition problem. When it died for good, at least it did it in town. Gabby trucked down the road to the nearest auto parts store for another unit, which was installed in pretty short order. He’s been reliable ever since. The mild but frustrating front end shimmy is expected to go with the old tire and while I have the wheel off for that, I will change the bolts that the speedometer sensor detects, which should stabilize the indicated speed. Change the headlight and I think Sponge Bob will be good for a while.

As for the Dragon trike, the two biggest things it needs are the shifter and the fenders, and arguably, the fenders could wait. The current shifter is such a pain to operate that it is difficult to properly tune the engine under and real driving conditions.

Replacing the shifter will involve welding on an alignment jig to bolt the new shifter to temporarily, cutting out all the old shifter parts, building a mount for the new shifter then removing the jig. The biggest question remaining is whether the shift lever can be easily removed from the new shifter to facilitate removing and installing the body.

While I have the body off for the shifter work, I need to clean up some wiring issues. Some of the wires are too short and since they plug in to the back of the fuse blocks, tension has resulted in some wires coming unplugged. Similarly, the wiring harness on the body needs to be secured better. I used sticky taped wire looms, but most of them didn’t last as long as it took to finish assembling the trike. Those looms need to be epoxied to the underside of the body.

A Prize Winner

I can’t believe I didn’t post anything about this when it happened. After all the work last September, I didn’t get to ride the dragon trike to a BTW benefit I was involved with, but I did tow it there and it won Best of Show *and* Best Engine.

Thanks to Bondo Joe Lane for both the prize winning paint and this picture of me and my goofy grin. ๐Ÿ™‚

Quick turbo inspection

I had a slightly slow start, but a productive day.

After welding one of the fenders back on Sponge Bob Square Trike and putting new fishtail ends on Gilbert’s exhaust, which involved replacing the mufflers with straight pipes ๐Ÿ™‚ , I spent a few minutes accessing the turbo to see whether or not it’s completely trashed.

At this point, it need cleaning, but looks good.

All I removed was the muffler and the intake duct. As determined by the borescope, the bottom of the intake was full of oil. A bit of oily sludge was still draining out after several minutes.

It appears to be corrosion-free, at least what I can see from here.

I love how tiny this thing is. Here it is, nearly obscured by my index finger.

I turned the impeller manually; it moves nicely, no obvious play. Turning the impeller also raised some more oily sludge from the bottom. It’s not a very efficient lift pump.ย I will definitely need to remove it for cleaning. I think I will contact Majestic Turbo in Waco and see what it costs to have them check it out.

Recon

While I haven’t done a whole lot on the bike lately, neither have I left it completely untouched.

Today, I received my borescope, purchased on eBay.ย At this point, I haven’t worked out a good way to photograph through it.

pv_618

Before the scope arrived, I borrowed a Rigid See Snake.ย This is basically a tiny camera with lights at the end of a three foot gooseneck, with a color monitor in the pistol grip. The camera module is about 3/4″ in diameter, so it wont through as small a hole as the borescope, but it’s way easier to share the vision.


The duct between the compressor and the surge tank is steel, presumably to withstand boost pressure better than the more typical neoprene. Peering into the duct, I saw bright surface rust, which worries me because I now must presume that the turbocharger has been exposed to raw weather.

I put the See Snake into the duct:

And past the rust, this is what I saw:

This is the pile of what I am guessing to be cypress leaves and lots of other trash that is sitting at the bottom of the duct between the compressor and the airbox or surge tank on the Seca. The round boundary at the edges of the pic is the bottom end of the duct, where the body of the duct and the coupler meet. The wide ring most visible in the lower right is the outlet duct of the compressor itself.

Without checking this first (and for the record, I was planning to pull the ducts and even the turbocharger out and check it anyway) this trash would have been blown up into the surge tank and on into the cylinders where it may or may not have caused any appreciable damage.

None of the pix came out good, but the other duct, between the airbox and the inlet of the compressor, has a substantial amount of standing oil in it, at the elbow where it turns towards the compressor.

Uh oh, I’ve got….. HAPPY CLUTCH!

With my apologies to Steve Martin…

I had to skip an evening, but we were released from work a couple hours early, so I have had time to get a bite to eat (skipped lunch today), get home, change clothes, finishe assembling the trike, test ride and adjust the clutch, all by about the time I would normally be getting home.

The new clutch works very well. Everything is very smooth. This throwout bearing may have been going out for longer than I had thought.

Sponge Bob Clutch Problem Resolved

I used my fancy new tool and removed the remaining shock absorber. It worked perfectly. ๐Ÿ™‚

I pulled the engine and saw that the throwout bearing had not, as I had suspected, jumped off the fork. Instead, I saw that the collar on the pressure plate had been ground off.

Some pieces of metal were recoverable, but mostly, there was a lot of shiny dust and a funky “burned barbecue” smell. The inside of the bell housing was coated with oil. My first thought was that the seal on either the engine or the transaxle was leaking.

None of the oil looks fresh, however. I recall that when the oil cooler event occurred, the top of the engine and transaxle were pretty much drenched in oil and I think that’s where it came from.

The throwout bearing itself had not jumped the rails, but you could tell that the surface didn’t look right.

Turns out that the bearing was not turning and the collar from the pressure plate had friction welded to the bearing race!

You can see the bearing race is completely hidden. For the entertainment value, I will see what forensic data I can gather and report back.

It’s no wonder the bearing failed, what with the inner race being off center and the balls scrambled inside the bearing.

I found that AutoZone carries the throwout bearing, for $37. They are about $15-18 at most places. AutoZone isn’t usually that high on any given item.

More importantly, while I have a new pressure plate leftover from the other trike, it looked like replacing the disk would be a good idea, what with all that oil. The disk also had a slightly strange wear pattern on it, seeming to wear most in a circle that would describe the center of the friction material. The contact side of the otherwise ruined pressure plate looked fine, but obviously it had to go.

AutoZone has a clutch kit which contains the clutch disk, pressure plate, throwout bearing, pilot bearing and a (redundant) pilot alignment tool. This whole assembly is $102 *and* carries a lifetime warranty. So I got one.

Nothing very magical about the installation from this point forward. I scraped as much of the slightly sticky dust off the flywheel as I could and vacuumed it away. Then I used a bunch of brake cleaner to ensure that the flywheel was clean and oil-free. After the brake cleaner, the pilot bearing needed grease.

Then I put the disk and pressure plate on and snapped a picture of it:

Looks like pretty much every other clutch, huh? ๐Ÿ™‚

It took pretty much a whole can of brake cleaner to get the bell housing clean. I found a few recognizeable bits of metal from the old pressure plate in there. I installed the new throwout bearing. Now that I’ve done it a few dozen times, I can remove and install the spring clips with minimal bloodletting.

Bolted the engine and transaxle back together and before I continued, I verified that the clutch will disengage. That was a problem with the Dragon trike’s clutch and I wanted to make sure the same thing didn’t happen here before I finished bolting up everything else and had to pull it out again!

I ran out of time and will need to finish the rest of it tonight.

Sponge Bob Break

Sadly, this is a pun. Not only does this post represent a break in the current storyline, it is also a lament that Sponge Bob is broken.

I swear, I’m not taking that trike to Arlington anymore. We took it Oklahoma and to the Hill Country twice and all over the metroplex. The clutch broke once in Oklahoma on it’s first journey, but regardless of all the other traffic, it has broken down three times in Arlington.

Good or bad, at least I’ve gotten good enough at riding it without the clutch that at least I wasn’t stranded in Arlington. This time.

So, I need to figure out what’s wrong this time. I suspect that the throwout bearing has jumped off the rails. There seems to be a delicate balance on exactly where the clutch arm needs to stop. Which is, of course, me saying that I’m sure it’s actually my fault, but I still suspect an Arlington connection.

Checking the throwout bearing is a fairly simple affair. Remove four wires, one fuel line and the four nuts holding the engine on and check it out.

To remove the engine, however, I need to remove the baja bumper. To remove the baja bumper, I need to remove the shocks. The new shocks are coilovers, which complicates their removal and installation because they need to be compressed to fit.

They make a tool to compress these sorts of springs. I have search for one locally to no avail and just have never gotten around to ordering one. So I was trying to figure out a way to compress the shocks since I will need to do this occasionally.

I first tried a ubolt extended with all thread, but there isn’t room on both sides of the shock for the all thread. I figured a way to do it with a couple of hand fabricated hooks. It took about 30 minutes to fashion the hooks and try it out to remove one shock. It worked pretty well, but one hook straightened out and failed while the shock was sitting on the bench. I knew the concept was good and just needed stronger hooks, so I made another with braces.


The hook on the left is designed to clear the spring. Were I to remake the hook on the right, I might offset the hole for the all thread so it would be parallel to the body of the shock, but I’m not sure that would really be necessary.

I might also add a brace at the far right and use a longer all thread so the wrenching surface would be easier to reach. That hook is on the bottom of the shock and moving the nut closer to the end would let it be reached more easily from below the trike.

As it stands, it works well enough to install and remove at least the one shock.

Once I was finished with that, decided I was too tired to tear into the trike and cleaned up the shop before things get out of hand. A few days of cutting and grinding makes a mess.

Maybe I wasn’t so tired after all because I also *finally* assembled a storage cabinet that I have had for enough months to wonder if it could be counted in years. It’s a nice big cabinet, and as expected, it doesn’t have enough shelves, but I can fix that.

It looks twisted in the pic, but it isn’t. I put a few things that have been sitting on the floor in it, as well as all the power tools that have been in a functional but ugly cabinet that I will be taking down. I think I have a place for the old cabinet. Where it is will go my band saw and drill press, which have also been sitting around on the floor a while.

Footpegs Continued

The #2 tip is enough bigger to get the job done, but I still had a LOT of trouble getting the inside corner of the 3 way intersection properly bonded.

Still, I think it will plenty strong. Nearly 50% of the gusset’s entire edge is secured.

I ran a sanding disk over it everywhere I could reach.

Perhaps I can use my little abrasive blaster to further clean the crevices.

Tomorrow, I pick up the ubolts and try it on for size. Assuming it works, on Monday I will drop it off for powder coating (which is preceded by a rather aggressive shot peening by a massive machine called the Wheelabrator, so I’m not sure why I am worried about sanding it) and that will nearly be that.

Picking it up and handling it reminds me of a crossbow….